gregf27
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posted on 27/7/08 at 08:32 PM |
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XE ignition module failing???
Still having a few hiccups on the XE in my F27
after a run of about 20 minutes , when i brake coming up to a junction or roundabout , the revs drop from around 900rpm til it stalls,I have to press
the accelerator down to keep the revs up, but it will keep stalling, unless I pull over and let it all cool down. then it starts again and behaves
itself until after 20 minutes or so,when it all happens again!!
the water temp creeps up too, and oil pressure drops.
I have replaced the oil pump, checked and replaced the king lead , I did swop over the bosch ignition module ( twin 45's on cav mk2 dizzy - so
no ecu) but it wouldnt even start, so I swopped it back again,
Would a failing ignition module cause the symptoms I have described??
or could it be the coil failing,
any ideas anyone?
spoiling my fun all this hassle in this lovely weather
Greg
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loggyboy
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posted on 27/7/08 at 10:25 PM |
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In my expereince a failed module would cause a complete hault to the engine. firing or a miss fire/ firing on 3 cylinders, rather than a iffy idle. I
would say check the idle valve but if ur on carbs you wont have one! so id look at carbs/setup 1st.
Mistral Motorsport
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Stu16v
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posted on 28/7/08 at 07:59 PM |
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Greg, do you want to borrow my dizzy/coil/module again? At least we know that is all 'known good' - you can try swapping one at a time
then?
Dont just build it.....make it!
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Stu16v
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posted on 28/7/08 at 08:01 PM |
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But TBH, with the symptoms you describe - I reckon the coil is the next thing that would be on my list of swaps...
Dont just build it.....make it!
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gregf27
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posted on 29/7/08 at 09:45 PM |
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Stu,
I have changed the coil over for a new one tonight( the old one looked quite corroded looking inside where the king lead fits!!), and await another
trial run!!
will give you a shout if any more probs!
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gregf27
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posted on 6/8/08 at 07:58 PM |
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All sorted - I think!!!
took the dizzy cap off to find the little black bit in the middle of it on the inside was missing!
so it must have been arcing between the the king lead and the rotar arm!!
replaced the cap with a new one and replaced the rotar arm too . runs a lot better now!!!
jeez its quick!!!
a lot better than me old pinto
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Stu16v
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posted on 6/8/08 at 10:10 PM |
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Jeez - nice one mate!
Welcome to the world of the XE (at last!)
Dont just build it.....make it!
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